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Mineral Processing Plant Micaceous Schist Ores Acid Cationic Method for Mica Process

Mineral Processing Plant Micaceous Schist Ores Acid Cationic Method for Mica Process

Acid Cationic Method Mineral Processing Plant

Micaceous Schist Ores Mineral Processing Plant

Mica Process Mineral Processing Plant

Lugar de origen:

China.

Nombre de la marca:

Hengyang

Certificación:

ISO9001

Número de modelo:

HC-615 y sus derivados

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Detalles del producto
Name:
Micaceous Schist Ores Acid Cationic Method for Mica Process
Capacity:
0.5-10t/h
OEM:
Accept
Color:
customize
Condition:
New
Condiciones de pago y envío
Cantidad de orden mínima
1
Precio
3000-150000
Detalles de empaquetado
Negociado
Tiempo de entrega
20 a 40 días
Condiciones de pago
T/T
Capacidad de la fuente
270 sistemas/mes
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86-371-56611369
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Descripción del producto

Continuous treatment of the graphitic-mica schist ore included grinding, classification, pre-concentration, conditioning, and flotation. The flowsheet for the process is shown in figure 4.

The ¾-inch dry-crushed ore was stored in an ore bin and withdrawn by a feeder onto a vibrating screen. The minus 4-mesh screen undersize passed to a spiral classifier to remove slimes. The spiral classifier overflowed to a 150-mesh vibrating screen. The minus 150-mesh undersize went to waste. The plus 4-mesh screen oversize, spiral classifier sands, and plus 150-mesh screen oversize passed to a rodmill. The ore was ground in the presence of sodium hydroxide to aid in removing and dispersing slimes. The plus 28-mesh trommel oversize consisted primarily of leaves, trash, and other organic matter and was discarded. The minus 28-mesh trommel undersize passed to a Humphreys spiral to partially concentrate the mica and remove part of the quartz. In addition to rejecting 28 percent of the weight of the ore with a loss of only 5 percent of the total mica, the spiral also rejected most of the pyrite, limonite, and other heavy minerals in the ore. The spiral rougher concentrate passed to a bowl-rake classifier for additional desliming. The bowl-rake classifier overflowed to a 200-

Mineral Processing Plant Micaceous Schist Ores Acid Cationic Method for Mica Process 0

mesh vibrating screen. The minus 200-mesh undersize went to waste. The plus 200-mesh screen oversize and the classifier sands passed to the graphite flotation circuit. A rough graphite product was floated with an alcohol frother, and cleaned once to reject an impure graphite product.

The graphite tailing was dewatered in a spiral classifier. The classifier sands passed directly to the subaeration-type flotation cells, where sulfuric acid for pH control and quartz depression was added. The amine collector (Azamine F10A) was also added in the first flotation cell. A rough mica concentrate was floated in a bank of three rougher cells. The rough concentrate was cleaned twice to produce a finished mica concentrate. The middling product, containing blocky mica, was returned to the rodmill for additional grinding. The flotation process accounted for a recovery of over 83 percent of the total mica in the ore in a product containing 98.7 percent mica. The summarized results of the test are given in tables 10 and 11.

Mineral Processing Plant Micaceous Schist Ores Acid Cationic Method for Mica Process 1Mineral Processing Plant Micaceous Schist Ores Acid Cationic Method for Mica Process 2

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